analog_programmer wrote on 2025-07-18, 07:54:
Anyway, it was necessary to replace all of these Hitano c(r)aps.
Oh absolutely, no argument about that. 😁
I mean, even if their ESR had gone up 10x, some circuits (e.g. linear regulators) could still tolerate that and operate fine. But when the capacitance goes so low (less than half), that's *not* good.
analog_programmer wrote on 2025-07-18, 07:54:
My next suggestion is for broken BGA GPU connection due to continuous overheating.
Well, these cards use leaded solder, so it's unlikely for the BGA solder between the GPU substrate and GPU PCB to have failed. Rather, it's usually where all the heat and stress is: between the actual GPU die and the GPU substrate (the square PCB on which the die is mounted on.)
That said, a "reflow" (reheat) process can still bring these back to normal operation.
Unfortunately, it just cannot be considered a permanent fix and the problem will likely come back again. My experience is that the lower the temperature the GPU is kept at after (while operating), the better the chance of the reheat "fix" to last... though also worth noting that I find that the more complex and larger the GPU die, the quicker the problem will come back. Luckily RV360 die is pretty small, so it should have a better chance of lasting longer.
analog_programmer wrote on 2025-07-18, 07:54:
Just adding a fan won't help. The problems begin when the card and GPU's heatsink become warm, not too hot.
Have you tried it, though?
FWIW, having a fan blowing on these cards can lower their idle run temps by at least 5C and more under load. So you might actually be able to see an improvement... or at least a delay in when the card starts to crash.
analog_programmer wrote on 2025-07-18, 07:54:
As far as i know Hitano c(r)apacitors are chineese (not even taiwanese) despite their japanese sounding name.
You know what, you might be right. It's been many years since I did my reading on those. In any case, all I remember is the same thing you said in your earlier post: they are crap and should be replaced anyways. 😁
analog_programmer wrote on 2025-07-18, 07:54:
Unfortunately Gigabyte card doesn't have any fan connector terminals. For now it runs fine.
It may run fine, but that's the problem with these: they are fine until they are just not. 😁
I need to dig out mine next time I'm in the countryside house and take a look at it for you. IIRC, there are a number of places where you can take 5V and 12V from and I think I even labeled it on mine. That said, on many cards (even if they have fan connectors), the easiest way for me to give their fan 7V is to solder new wires to spots that have 5V and 12V. (And before anyone says that's not a proper/good way of wiring things, for small loads such as a fan or three, it's fine. Almost all of the computer hardware I have from the early 2000's has a fan wired like this one place or another. Haven't had a problem with it in over 20 years. And I don't expect it to. The person I actually learned this from learned it from doing industrial wiring... so it's not necessarily an unsafe "hack".)
analog_programmer wrote on 2025-07-18, 07:54:
Reballing is not for me, but I can try BGA GPU connections "resoldering" with hot air gun...
Yup, that's the plan here anyways.
A reball would be a waste of time as it won't help anything anyways, since such issues are not the BGA between the substrate and card's PCB that fails.
analog_programmer wrote on 2025-07-18, 07:54:
As for my old and problematic PSUs, I really have to restore one ATX unit for older systems (with PIII or Athlon (XP) motherboards) testing. I managed to find two very similar circuit diagrams for LC-B250ATX PSU, which I think is ATX ver.1.x standard. This weekend I'll start to reassemble it. I also have one ATX ver. 2.1 standard AT-2005B PSU, which is in even worse state (I tink I keep all of it's main components) and I can't remember which MOSFET or double diode where goes on the PCB, but for now I'm not in need to restore it.
LC-B250ATX is a basically a very low-end and cost-cut Deer/Solytech unit. But their design is overall solid and workable with. So if that's what you have for your PSU (or another similar LC-BxxxATX unit), they make for decent ATX 1.0 PSUs with all of the proper parts installed. Namely, L&C puts much smaller and/or less caps on the output of these PSUs, along with often omitting the "PI" coils/inductors between the caps. Adding these back and making sure the 3.3V and 5V rail get at least 2x 2200 uF low ESR caps and the 12V rail at least 2x 1000 uF caps is really all that's needed for these PSUs to be decent again... well that and a full recap of the small caps too, along with the 5VSB circuit, as all of those will bring nothing but problems if disregarded.
FWIW, I have two LC-B300ATX units. One I semi-restored (added the proper caps on the output and also the missing PI coils), but didn't fully recap. The other is still in parts in one of my parts boxes. Going to restore it eventually too, despite having more than enough 5V-heavy PSUs I would ever need. At $0.50 (1 Lev) on the flea market here, it's hard to pass them up sometimes. Just the two BJT transistors inside it are worth more. 😀
shevalier wrote on 2025-07-18, 11:27:
This is while the capacitors at least somewhat correspond to the datasheet.
True.
shevalier wrote on 2025-07-18, 11:27:
If the capacitor ESR has increased 10 times (from 40 mOhm to 0.4 Ohm), then no amount of heating will help it.
Well, you might be surprised of how much the ESR can vary on failed caps then. I've seen them improve their ESR by 5-10x on a regular basis just from heating them with the soldering iron or with a hot air gun (usually heating them anywhere from 40-55C T-case).
So heating them most definitely can help them get "better" (temporarily anyways.)
What the heating won't and can't help is to restore lost capacity due to "consumed" foil plates from an unstable electrolyte... and ultimately it's this and not so much the ESR increase, that brings electronics circuits from functional to non-functional state... though that will depend greatly between different circuits. For example, if a problematic cap is filtering a rail that also has ceramic caps as part of the filtering, then an increase in the ESR of the electrolytic cap won't be that problematic... not until the filter's whole capacitance becomes so low that it starts messing with the compensation on the voltage feedback loop of the controller circuit. But in other circuits like the small "start-up"/bootstrap capacitors of standby power supplies, the ESR of these small electrolytic caps (which are responsible for filtering the primary auxiliary winding and also storing a charge at the circuit's "boot up" loop) may play a much greater role in when the circuit stops functioning.
So it really depends on the actual circuit.
That said, most electronics circuits are overall designed to be quite tolerant of the ESR of electrolytic caps.
Since the 2-4x increase in ESR/impedance with temperature decrease (from 20C to -10C) is really more of an average value than a hard number, and since the capacitors are expected to degrade over time, many (properly-designed) circuits will usually have enough overhead to easily tolerate a 10x increase in the ESR values. Thus, heating up caps that have gone bad (but not completely bad like the Hitano's above with almost non-existent capacity 😁 ) can sometimes "restore" a device, at least for a quick test.
shevalier wrote on 2025-07-18, 11:27:
As for checking the resistors, it's a good idea unless they are 0402. Then you either need to be young or have a microscope.
But being young is better 😀
Yeah, I can start to feel the weight of this statement a lot more now as time goes by.
FWIW, I can still see and measure these fine without a need for magnifications... but it's getting harder. 10 years ago, I wouldn't even blink once when having to work with these. Now I have to "train" my eyes for a few minutes before I can finally get them to focus... and it's still not as clear as I'd like it. But I'll take it.